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After I (more or less) finished my 1966 Volkswagen Fastback the "Volksback", it was time for another challenge, here it is!

Samstag, 12. April 2014

oil cooler thread repair - the sequel...

I wasn't too sure about the thread repair, so I borrowed a Helicoil repair set:

 ... drilled and tapped the special thread size...
... and inserted a helicoil insert, now I feel safe:

this will last forever!

and here another pic of the oil cooler adaptor with the M6/M8 bolts already inserted and loctite'd:

During the assembly I noticed this problem: No thread for the oil pressure switch:
 but a few hours later I had this: a nice, clean M10x1 thread:

 next on the list was a new oil cooler:
... more soon

Freitag, 11. April 2014

.. what I didn't mention yesterday...

During my bolt repair action I had another incident which I forgot to mention yesterday:
... as if there wasn't enough trouble, the drill bit also broke! fortunately I could safe it with a plier!
At the end of day the I wasn't to sure about my repair and re-did it again - more of this later...

Donnerstag, 10. April 2014

cylinders, heads and oil pump - and some headaches...

After I found out about the too high compression ratio, I had to use 0,5mm shims under the cylinders to reduce the compression to a final and healthy 9,3:1
 I also managed NOT to forget the (type 3) cooling tins!


a set of new push rods 

and of course, new push rod tubes with a slight drip of sealant


just for the record: cylinder head details and valve sizes:




a re-surfaced oil pump cover (original VW part - which is still the best)

a new oil pump followed soon:


with the slimmest available paper seal, to keep the oil pressure on a good level

oil pump finished!

a mechanical fuel pump was next on the list.

Next task: the oil cooler - which gave me headaches...
The upright adaptor has M8 threads, but the holes in the case are for M6 bolts - then again, the threaded bolt in the case is 6mm and the adaptor has a hole for M8


too fat bolts...

 o.k., first step: remove the bolt from the case - easy- isn't it?

Damn - this wasn't suppose to happen!
How could this happen? I used an extractor tool?

This is the problem: The cheap tool broke and in turn the bolt snapped!

 So, after some swearing, I drilled out the remains of the old M6 bolt...

 Here is the remedy for the thread problem: Bolts with M6 AND M8 threads. A special thanks to Thomas for a nice and fast job!

Here is the new, stepped bolt already loctite'd into the case
The other 2 bolts will be used in the adaptor...
Thanks to this trick I can later use the engine in original Type 3 configuration again!

Dienstag, 1. April 2014

short block finished - next step: long block assembly!

After I lubed all bearings, coated the cam lobes and lifters with Molykote 3402-C and cleaned the sealing areas really religious, I finally assembled the halfs and torqued all bolts to the correct values. I used sealant under all washers and nuts - in hope for a clean, leak free engine.

Then I started the piston + cylinder assembly.


Every component got a bath in my ultra sonic cleaner to make sure they are really clean:


the pistons are lubed, the wrist pin clips are positioned with the sharp edge to the outside, I de-burred the edges from the stamping process prior assembly:

the cylinders required a little persuation for a good fit - of course only with a "soft" hammer!

as the seats for the cylinders were machined for a nice overall sealing surface, I have almost "0" back lash, the piston ends exactly where the cylinders ends - not good for a healthy compression ratio!

In order to calculate the compression ratio I cc'ed the heads. Starting with 60ml of motor oil in clean, new mega-syringe:
(the pic shows it filled to 61 cc - but I adjusted it to exactly 60cc before I started)
the combustion chamber, topped of with oil - spark plug hole sealed flush: 


... and the rest in the syringe: exactly 10ml

So, according to the helpful website of CSP, which provides an easy way to calculate the CR ->  look here  <- we need these values:
bore: 90.5 mm
stroke: 69 mm
head volume: 50 ccm
back lash: 0 mm
result: CR: 9,88  which is a little too high - so I will double check all values and maybe use 0,5mm shims to reduce the CR to 9,34:1 which is almost exactly my target (9.5:1)!

 

Sonntag, 30. März 2014

engine assembly, again

no big news, but some info regarding the stuff I used on the lifters and the cam surface:

I found a fuel pump block off plate, deep in my parts stash - I am still undecided if I use the mechanical VW pump or an electric one...

Later this week: short block assembly!

Oh - of course I was at the Techno Classica in Essen, the biggest classic cars show on earth - according to the organizers...
All I can say, it is not cheap to go there, the prizes for classic cars are unreal and it is more and more a meeting for the "rich and famous" - unfortunately!
I still found a few parts, but almost all of the VW part dealers are not there any more, strictly Porsche, Mercedes, Ferrari and other high class classics...
Here is what I found:
a new cushion for my car jack, a 38mm socket with 3/4" drive, a new coil and some electric stuff.

Dienstag, 25. März 2014

... more assembly pics

Here is the marking on the Schleicher cam:
RO248.7 = which equals 296°; 9 mm lift

set up of axial play measurement: 

current reading is 0,12mm - but it wasn't torqued to the max, so I expect ~0,1 axial play

another -very easy- job was to add a missing bolt for the oil strainer plate:
(of course loctite'd)

 result:

In the meantime I test-fitted the housing and internals several times, the next step is to finally bolt the halfs together, using the correct sealant. Porsche recommends Loctite 574, so I will use this, too. If it is good enough for a Porsche it should be just right for my VW as well ;-)

Samstag, 22. März 2014

engine assembly, continued

Here are a few more goodies:

chromoly cylinder studs, a good quality engine gasket set and the CSP oil pressure valve screws with a nice allen head instead of the mega slot...

the story so far: